Skripsi
EVALUASI KINERJA SIPHON STRING PADA SUMUR X-28 LAPANGAN Y PT. PERTAMINA EP ASSET 3 CIREBON, JAWA BARAT
PT. Pertamina EP Asset 3 have a many optimization project in one time. There are two ways of optimization work for achievement of production targets set by PT. Pertamina EP Asset 3. Optimization Project work with Well Intervention (Intervensi Sumur) to increase production, in which case no one uses Rig Service such as Acidizing, Fraci'uring, Surfactant, etc. There also are not used rig (Rigless), by adding tubing by inserting Siphon String. Then Optimization job that does not require Rig is Siphon String Installation. Oil Recovery that by use Siphon String will be more optimal. In theory, using Siphon String can be increase production until 100%, it can be seen from IPR and OPR Curve Nodai Analysis results by looking at the sensitivity Tubing. It happens because in X-28 is a Natural Flow wells that produce intermittent. Intermittent where the production cycle and Shut-In cycle conducted sequentially in the respective period of time. Average production before installation Siphon String is 20 BFPD, after Siphon String Installation production is continuous flowing cmd increase production up to 90% to 38 BFPD.
Inventory Code | Barcode | Call Number | Location | Status |
---|---|---|---|---|
1707000309 | T141044 | T1410442017 | Central Library (References) | Available but not for loan - Not for Loan |
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